Skip to main navigation Skip to main content
  • E-Submission

JKSPE : Journal of the Korean Society for Precision Engineering

OPEN ACCESS
ABOUT
BROWSE ARTICLES
EDITORIAL POLICIES
FOR CONTRIBUTORS

Page Path

2
results for

"Yeong Chun Kim"

Article category

Keywords

Publication year

Authors

"Yeong Chun Kim"

Articles
Design and Verification of Multi-Step Blade Tip Clearance Control System for Large Gas Turbine Using Hydraulic Pressure
Yeong Chun Kim, Seok In Cho, Yang Uk Cho, Heui Joo Park
J. Korean Soc. Precis. Eng. 2020;37(5):347-353.
Published online May 1, 2020
DOI: https://doi.org/10.7736/JKSPE.019.113
In the gas turbine, the clearance between the blade tip of the rotor and the inside of the stationary casing varies depending on the rotation of the rotor and the heat output of the combustor. Accordingly, the assembly clearance is determined, and the leakage of the gas occurs because of the gap during operation, affecting the efficiency of the system. Thus, designers use a variety of techniques to optimize this clearance, a typical method that reduces the relative variation of the clearance using heating and cooling mechanisms. In this study, we developed a method to control the blade tip clearance through the axial movement of the inclined blade without using heating and cooling mechanisms. Recently, we designed an advanced blade tip clearance control system that can control multi-step, not on-off control, to apply to large gas turbines developed by Doosan. The designed system is hydraulic and can be used with a maximum thrust of 100 tons, and the desired displacement can be moved in multiple stages as required. We have completed the reliability verification of the entire lifecycle level and applied it to the newly developed gas turbine.
  • 5 View
  • 0 Download
The large gas turbine rotor used for power generation has a structural characteristic comprising a shaft, disk, and blade assembled to the disk. Because the start/stop is repeated, the tightening force may be reduced in the process of repeating the tightening force between the tie rod and the disk. When the tightening force falls below the threshold, changing the critical speed, increasing the vibration, or in extreme cases, the rotor may loosen and cause a major accident. Also, it is imperative to continuously maintain the proper tightening force because the thread of the tie rod is damaged when the tightening force exceeds the yield stress condition of the tie rod. In this paper, the gas turbine rotor system is modeled and simplified to identify the control variable of the tightening force of the tie rod bolts of the rotor. For verification, a simplified model of the gas turbine rotor was designed, manufactured, and verification tests were conducted to confirm the adequacy of the calculation method. As a result, the tightening force decreased as the stiffness of the pressing disk decreased, so the stiffness of the pressing disk should have a stiffness range similar to that of the tie rod.
  • 4 View
  • 0 Download